Video showing the Overbot as rigged to run the DARPA Grand Challenge in 2005. Video is provided courtesy of J. Nagel of SVORA.


 

Multimedia

Video showing the Overbot on its first autonomous run at UC Santa Cruz, August 2006. The Overbot was not able to keep its path due to a sensor failure.
 

Video showing the Overbot on its 2nd autonomous run at UC Santa Cruz, August 2006. The Overbot engine dies at the turn point, aborting the run.



Video showing the Overbot on its 3rd autonomous run at UC Santa Cruz, August 2006. The Overbot engine dies after beginning its 3 point turn to sense obstacles after the turn point.